Does anyone have an update on the Marchand Unit in North Mahoning Township. One unit is producing and four additional permits are on the books.
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Permalink Reply by farmgas on April 4, 2018 at 4:00pm Previously well #3I was drilled in 2013 and was a producing marcellus well. In dep inspections & violations reports, there is a constant mention after the Utica was drilled that well 3I is drilled and appears equipped for production. Could that well have been reworked while the rig was on the pad drilling the Utica well? Just wondering...
SK - could choking back of the Utica produce these numbers? Why would they do that?
Permalink Reply by BW_Appalachia on April 4, 2018 at 11:13pm Could be choked back due to pipeline capacity in the area.
Permalink Reply by farmgas on April 5, 2018 at 1:21am
Permalink Reply by farmgas on April 5, 2018 at 3:21am
Permalink Reply by farmgas on April 5, 2018 at 4:11am
Permalink Reply by farmgas on April 5, 2018 at 7:43am So, we shouldn`t be too quick to judge this report.
Here is the completion report.
Got it, read it. From what (admittedly limited amount) I know, this does not look too promising for a Super-Well. Except if there's something not obvious and a new way of flowing them back and completing them that chokes back the 24 hr rate to minimize reservoir damage and maximize EUR.
Since CNX hit 3 home runs in their first 3 at bats, I suppose it's unreasonable to expect them to continue the streak forever... but still
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